Accident Eurocopter AS-350BA N906BA,
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ASN Wikibase Occurrence # 285571
 
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Date:Friday 19 September 2008
Time:16:45 LT
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different    
Eurocopter AS-350BA
Owner/operator:Liberty Helicopters
Registration: N906BA
MSN: 1479
Year of manufacture:1981
Total airframe hrs:12803 hours
Engine model:Turbomeca Arriel 1B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Linden, New Jersey -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Training
Departure airport:Linden Airport, NJ (LDJ/KLDJ)
Destination airport:Linden Airport, NJ (LDJ/KLDJ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight instructor was monitoring the student pilot during a 180-degree autorotation as part of the flight training. The maneuver was entered at 700 feet above the ground and at 100 knots. Once the intended spot was made for the 'power-on' recovery, the flare was started. As the flight instructor advanced the fuel flow control valve into the flight position, the helicopter started to settle and the low rotor speed horn came on. The flight instructor took over the controls advising the student pilot that it was going to be a run-on landing. During the landing, while in the ground run, the nose of the helicopter pitched forward as the skids dug into the mud. The flight instructor pulled back on the cyclic to prevent the blades from contacting the ground. The helicopter came to rest in the upright position in the grassy area. Post accident inspection of the helicopter's main rotor system revealed that the 2,167 hours time in service Starflex component had two of its three arms fractured. Examinations of the fracture surfaces revealed no indications of any pre-existing damage to the areas. The fractures were consistent with overstress and unusual loads, which were produced during abrupt flight control inputs with low main rotor RPM.

Probable Cause: The flight instructor's delayed remedial action (flight control inputs) during a practice autorotation/run-on landing resulting in fracture damage to the main rotor system Starflex.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA08LA199
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

NTSB MIA08LA199

Location

Revision history:

Date/timeContributorUpdates
02-Oct-2022 11:42 ASN Update Bot Added

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