ASN Wikibase Occurrence # 285845
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 17 July 2008 |
Time: | 07:40 LT |
Type: | Cessna T210M |
Owner/operator: | |
Registration: | N6882B |
MSN: | 21062850 |
Total airframe hrs: | 4900 hours |
Engine model: | Teledyne Continental TSIO-520 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Van Horn, Texas -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Fort Davis, TX |
Destination airport: | Van Horn-Culberson County Airport, TX (VHN/KVHN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot positioned the landing gear handle to the "gear down" position in preparation for landing. The gear did not extend and the circuit breaker popped. His attempts to reset the circuit was unsuccessful. The pilot then turned toward an unpopulated, desert area and attempted to lower the landing gear through the hand pump. There was no pressure on the pump handle and it was determined that the hydraulic reservoir was low. The pilot, with the assistance of his passenger, opened the reservoir and added water to regain pressure and extend the landing gear. The gear appeared to be down with a visual check but there was no "down and locked" indication on the instrument panel. The pilot diverted his attention inside the cockpit in an attempt to troubleshoot the system. During this time, the airplane impacted the ground in a near level attitude. The nose gear was torn off, the propeller was damaged, and the left wing was substantially damaged. The airplane came to rest in the upright position. The pilot and his passenger were not injured and were able to egress unassisted. The pilot stated in the Pilot/Operator Report that the accident could have been prevented if he had remembered to keep flying the airplane.
Probable Cause: The pilot's failure to maintain altitude due to his diverted attention. Contributing to the accident was complications manually extending the landing gear.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW08CA191 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB DFW08CA191
Location
Revision history:
Date/time | Contributor | Updates |
02-Oct-2022 15:56 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation