ASN Wikibase Occurrence # 285987
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Date: | Sunday 8 June 2008 |
Time: | 19:30 LT |
Type: | Beechcraft A36 |
Owner/operator: | |
Registration: | N7214Y |
MSN: | E-2169 |
Year of manufacture: | 1984 |
Total airframe hrs: | 3214 hours |
Engine model: | Continental IO-550-B1F |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Grand Rapids, Minnesota -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Falls International Airport, MN (INL/KINL) |
Destination airport: | Minneapolis-Flying Cloud Airport, MN (FCM/KFCM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that about 40 minutes into the flight he heard a loud noise followed by a rapid deceleration of the engine, and then a "distinct bang." The windshield was immediately covered with a film of oil, completely obstructing forward visibility. He established a descent at best glide airspeed and established a course for the nearest suitable airport. During the descent, the engine continued to run rough and smoke entered the cockpit. It became apparent to the pilot that he did not have enough altitude to reach the airport. He attempted to increase engine power in order to slow the descent; however, the engine seized shortly afterward. He set up for a forced landing to a clearing adjacent to a set of power lines. During the forced landing, the airplane impacted trees and a utility pole, which separated the left tip tank and left aileron from the airframe. The airplane slid approximately 50 feet and came to rest upright. A postaccident inspection revealed that the propeller assembly had separated from the engine propeller flange. The propeller flange appeared intact. The propeller assembly was not recovered. Two propeller bolt fragments and one propeller alignment pin fragment were recovered from the engine cowling. Examination of the fracture surfaces revealed features consistent with reverse bending fatigue cracking. In addition, the washer faces of both nuts were worn and polished consistent with relative movement against the crankshaft flange. Maintenance records indicated that the propeller spinner bulkhead was replaced approximately one year prior to the accident in order to comply with a manufacturer's service letter. At the time of the accident, the propeller assembly had accumulated 1,906 hours total time in service, with 235 hours since replacement of the spinner bulkhead. About 531 hours had accumulated since overhaul of the propeller assembly.
Probable Cause: A loss of engine thrust due to the propeller separating from the aircraft as a result of fatigue failure of the propeller attachment bolts caused by the insufficient torque of the bolts during installation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI08LA154 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB CHI08LA154
Location
Revision history:
Date/time | Contributor | Updates |
02-Oct-2022 18:02 |
ASN Update Bot |
Added |
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