ASN Wikibase Occurrence # 286056
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Date: | Friday 23 May 2008 |
Time: | 15:45 LT |
Type: | Bellanca 14-19-3 |
Owner/operator: | Private |
Registration: | N7640E |
MSN: | 4143 |
Engine model: | Continental IO-470F |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | N. Little Rock, Arkansas -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | North Little Rock Municipal Airport, AR (KORK) |
Destination airport: | Gulf Shores-Edwards Airport, AL (GUF/KJKA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Prior to the flight, the airplane's fuel tanks were topped off with fuel, and the airplane pre-flight was normal. During initial takeoff climb approximately 200 feet above ground level (agl), the pilot retracted the landing gear and the engine lost power. Prior to the loss of engine power, the pilot did not hear a bang, sputter, or any indication of an engine problem. The pilot attempted to restart the engine; however, the restart was unsuccessful. The pilot initiated a forced landing and tried to land on the remaining runway surface. The airplane touched down off the runway surface, impacted terrain, and came to rest upright. Examination of the airframe and engine showed that the mixture and throttle cables were routed incorrectly, and the two cables were longer than the original cables. The original drawings showed that the cables exited the firewall and were routed up to the center cylinders and looped back to the fuel control unit. The accident airplane cables exited the firewall and were routed up to the forward cylinders (in proximity of the nose landing gear retraction assembly), and then looped back 180 degrees to the fuel control unit. The fuel control unit was mounted under and aft of the engine. The inspector noted contact with the mixture cable and the nose landing gear retraction assembly. During the landing gear retraction, the mixture cable was snagged by the gear retraction mechanism and disrupted the fuel system which resulted in the loss of engine power.
Probable Cause: The loss of engine power due to the incorrect and improper installation of throttle and mixture cables by unknown maintenance personnel.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN08LA095 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB DEN08LA095
Location
Revision history:
Date/time | Contributor | Updates |
02-Oct-2022 19:06 |
ASN Update Bot |
Added |
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