ASN Wikibase Occurrence # 286270
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Date: | Wednesday 27 February 2008 |
Time: | 01:41 LT |
Type: | Cessna 210L |
Owner/operator: | Flight Express Inc |
Registration: | N5489V |
MSN: | 21060961 |
Year of manufacture: | 1975 |
Total airframe hrs: | 14077 hours |
Engine model: | Continental IO 520 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tampa, Florida -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | Columbia Metropolitan Airport, SC (CAE/KCAE) |
Destination airport: | Tampa International Airport, FL (TPA/KTPA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While inbound to land, the pilot lowered the landing gear using the normal system and the nose and left main landing gears went into the down and locked position; however, the right main landing gear did not due to a false down-and-locked indication caused by a malfunction of the right main landing gear down-and-locked switch. As such, the pilot observed a green light indicating that all landing gears were down and locked and continued the approach. During the landing roll the right main landing gear collapsed. Postaccident examination revealed that the malfunction of the right down-and-locked switch was caused by a bent plunger, which shut off the electrically-driven hydraulic pump before the right gear went into the down and locked position. Since 1992, the right main landing gear down-and-locked switch had been replaced six times, with the latest replacement occurring in October 2004. The airplane had been operated for 2,082 hours since the latest switch replacement. Additionally, the operator performs gear rigging testing every 300 hours. The latest rigging check occurred on November 15, 2007. The airplane had accumulated approximately 218 hours since then at the time of the accident.
Probable Cause: The malfunction of the right main landing gear down-and-locked switch.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA08LA066 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB MIA08LA066
Location
Revision history:
Date/time | Contributor | Updates |
03-Oct-2022 08:10 |
ASN Update Bot |
Added |
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