Accident Beechcraft 35-A33 N4334W,
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ASN Wikibase Occurrence # 286820
 
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Date:Friday 10 July 2009
Time:09:15 LT
Type:Silhouette image of generic BE33 model; specific model in this crash may look slightly different    
Beechcraft 35-A33
Owner/operator:
Registration: N4334W
MSN: CD-331
Total airframe hrs:8406 hours
Engine model:Continental IO-470-J
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Las Vegas, New Mexico -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Saint Johns Municipal Airport, AZ (SJN/KSJN)
Destination airport:Las Vegas Airport, NM (LVS/KLVS)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
After a cross-country visual flight rules flight of one hour and 40 minutes, the pilot was landing at an airport with a surface elevation of 6,877 feet mean sea level. While on downwind for landing the pilot extended the landing gear and flaps, and set the engine power at 1,700 rpm. A witness at the airport heard the engine 'sputtering,” then the engine failed and restarted twice before he heard the engine fail completely. The pilot executed a forced landing to a field one mile south of the airport and the airplane flipped inverted during the impact with terrain. The airplane was substantially damaged by the impact forces and the post-impact fire. The two occupants were seriously injured. The investigation revealed that adequate fuel was present, with symmetrical fire damage to both wings. The engine was tested at the manufacturer's facility and during the first start the engine started normally on the first attempt without hesitation or stumbling. The engine rpms were advanced in steps to 1200 rpm and held for five (5) minutes to stabilize. The engine throttle was advanced to full open position and held for five minutes to stabilize. The engine throttle was rapidly advanced from idle to full throttle six times. Throughout the test phase, the engine accelerated normally without any hesitation or interruption in power and demonstrated the ability to produce rated horsepower.

Probable Cause: The loss of engine power for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN09FA430
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB CEN09FA430

Location

Revision history:

Date/timeContributorUpdates
03-Oct-2022 16:35 ASN Update Bot Added

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