This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 21 April 2009 |
Time: | 12:55 LT |
Type: | Cessna 208 Caravan I |
Owner/operator: | Greystoke Engineering Inc |
Registration: | N208JW |
MSN: | 20800166 |
Year of manufacture: | 1989 |
Total airframe hrs: | 14056 hours |
Engine model: | Pratt & Whitney Canada PT6A-114 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Frederick, Maryland -
United States of America
|
Phase: | Taxi |
Nature: | Ferry/positioning |
Departure airport: | Winchester Regional Airport, VA (KOKV) |
Destination airport: | Frederick Municipal Airport, MD (FDK/KFDK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the landing roll, with the power lever at idle, the pilot heard a 'pop,†followed by indications of the engine 'spooling down.†He exited the runway and observed smoke coming from the engine compartment. Thinking this was residual fuel, he 'spooled the engine.†Realizing there was a fire, he called for assistance and shut off the fuel selectors and firewall shutoff valve. After the accident, a FAA inspector examined the airplane and reported extensive thermal damage to the fuselage sub-frame and evidence of an engine fire. Numerous engine turbine blades were found on the pavement adjacent to where the fire occurred. A disassembly and inspection of the engine revealed that one or more of the compressor turbine (CT) blades failed. The engine was overhauled about 6 hours prior to the accident. The CT blades were manufactured under the FAA Parts Manufacture Approval (PMA) program. Extreme heat damage obliterated the fracture surfaces of the blades, therefore the reason for the blade failure(s) could not be determined. A functional test of the fuel control unit (FCU) revealed the Sg (specific gravity) dome, high idle stop screw, and minimum flow stop were set above the recommended range, which would result in higher than normal fuel flow. The FCU adjustments appeared to be made after the overhaul, however it could not be determined when the adjustments occurred. Although the higher than normal fuel flow setting probably did not result in the CT blade failures, it could have exacerbated the thermal damage and fire.
Probable Cause: A loss of engine power due to the failure of one or more compressor turbine blades for an undetermined reason.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09LA269 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB ERA09LA269
Location
Revision history:
Date/time | Contributor | Updates |
03-Oct-2022 19:43 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation