Accident Cessna 152 N6566P,
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ASN Wikibase Occurrence # 287198
 
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Date:Sunday 18 January 2009
Time:14:00 LT
Type:Silhouette image of generic C152 model; specific model in this crash may look slightly different    
Cessna 152
Owner/operator:Dean International Inc.
Registration: N6566P
MSN: 15285034
Total airframe hrs:7906 hours
Engine model:Lycoming O-235-L2C
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Wauchula, Florida -   United States of America
Phase: En route
Nature:Private
Departure airport:Brooksville-Hernando County Airport, FL (KBKV)
Destination airport:Miami Executive Airport, FL (TMB/KTMB)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was climbing to 7,500 feet mean sea level when the engine started vibrating. The engine temperature increased and the engine stopped. The pilot realized that he could not make an airport and made a forced landing to a phosphate field. Examination of the engine revealed that it contained 6 quarts of dark black oil. The oil filter was removed and contained metallic contamination. Disassembly of the engine revealed dirt particle embedment on the Numbers 1 and 2 cylinder connecting rod bearings. The Number 3 connecting rod bearing was found disconnected from the crankshaft, with only small steel fragments remaining. The No. 3 connecting rod cap and associated broken rod bolts displayed overload signatures. The Number 4 connecting rod remained attached to the crankshaft and displayed heavy heat damage consistent with oil starvation. The operator reported that its maintenance personnel were performing oil changes during the 100-hour inspections. Lycoming Mandatory Service Bulletin 480E states that engines with a full-flow filtration system are required to have the oil changed at 50-hour intervals.

Probable Cause: A loss of engine power due to failure of the Number 3 connecting rod due to oil contamination. Contributing to the accident was the insufficient oil change time intervals performed by company personnel.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA09LA146
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB ERA09LA146

History of this aircraft

Other occurrences involving this aircraft
12 June 1983 N6566P Private 0 Milwaukee, WI sub

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 08:18 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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