ASN Wikibase Occurrence # 287262
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Date: | Saturday 17 November 2012 |
Time: | 00:05 LT |
Type: | Beechcraft 35-B33 Debonair |
Owner/operator: | Westchester Flying Club |
Registration: | N8519M |
MSN: | CD-628 |
Total airframe hrs: | 11298 hours |
Engine model: | Continental IO-520 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | White Plains, New York -
United States of America
|
Phase: | Approach |
Nature: | Executive |
Departure airport: | Tarentum, PA (9G1) |
Destination airport: | White Plains-Westchester County Airport, NY (HPN/KHPN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On final approach for landing, the pilot observed that the airplane was high, and he performed a slip in order to lose altitude. During the maneuver, the engine lost power, and the pilot performed a forced landing to a parking lot. Postaccident examination revealed the fuel selector switch was in the off position; however, the pilot said that, after the accident, he turned the fuel selector from an unknown position to OFF and that he could not recall the prior position. The examination also found that the right wing fuel tank contained about 14 gallons of fuel, and the left tank was empty. Although the left wing tank was ruptured during impact, no evidence of fuel leakage or odor was found at the site. The airplane was equipped with a non-standard engine and propeller and did not have a Supplemental Type Certificate for the installation. Further, the pilot did not have fuel consumption information for the current engine-propeller installation; thus, the pilot likely misjudged the fuel consumption for the flight. It is likely that the fuel selector was positioned to the left tank, which had become very low on fuel. The slip maneuver aggravated the low fuel condition of the left wing fuel tank, and the airplane was starved of fuel, which resulted in the loss of engine power. Additionally, the pilot's failure to utilize the auxiliary fuel pump per the pilot operating handbook during air start most likely prevented the engine from restarting. Postaccident examination revealed no anomalies that would have precluded the normal operation of the airplane or engine components.
Probable Cause: The pilot's improper fuel management and his excessive slip maneuver, which led to fuel starvation and a total loss of engine power, and his failure to activate the electric boost pump during the attempted engine restart.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA13LA060 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB ERA13LA060
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 09:08 |
ASN Update Bot |
Added |
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