ASN Wikibase Occurrence # 287595
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Date: | Monday 9 July 2012 |
Time: | 16:00 LT |
Type: | Cessna 172S |
Owner/operator: | Gateway Aviation |
Registration: | N680MA |
MSN: | 172S8202 |
Year of manufacture: | 1999 |
Engine model: | Lycoming IO-360-L2A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Allentown, Pennsylvania -
United States of America
|
Phase: | Take off |
Nature: | Training |
Departure airport: | Allentown Queen City Municipal Airport (KXLL) |
Destination airport: | Allentown Queen City Municipal Airport (KXLL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While the student pilot was conducting touch-and-go landings, about the time of power application after landing, the airplane veered left and departed the runway onto the adjacent grass. The airplane subsequently struck a sign, impacted a gopher hole, and came to rest near a berm, sustaining substantial damage to the airframe and horizontal stabilizer. Three distinct tire tracks were visible in the grass up to the gopher hole. A postaccident examination of the left main landing gear assembly revealed overstress fractures from a single loading event, which was likely the impact with the gopher hole; no preimpact mechanical malfunctions or failures that would have precluded normal operation were found. FAA guidance indicates that an abrupt application of power may result in the airplane yawing sharply to the left. It is likely that at the application of takeoff power, the student pilot failed to apply an appropriate amount of rudder correction and the airplane departed the runway. The flight instructor did not recognize the student's failure to maintain directional control in a timely manner and failed to take appropriate remedial.
Probable Cause: The student pilot's failure to maintain directional control during a touch-and-go takeoff, which resulted in a runway excursion and a subsequent impact with a gopher hole, and the flight instructor's inadequate supervision of the student pilot and his delayed remedial action.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA445 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB ERA12LA445
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 12:30 |
ASN Update Bot |
Added |
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