Accident Cessna 170 N3812V,
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ASN Wikibase Occurrence # 287676
 
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Date:Friday 15 June 2012
Time:17:15 LT
Type:Silhouette image of generic C170 model; specific model in this crash may look slightly different    
Cessna 170
Owner/operator:Hart William C
Registration: N3812V
MSN: 18670
Total airframe hrs:3969 hours
Engine model:Continental C145 SERIES
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Biddeford, Maine -   United States of America
Phase: En route
Nature:Private
Departure airport:Biddeford, ME (B19)
Destination airport:Sanford Airport, ME (SFM/KSFM)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot/owner and his instructor, the preflight inspection and the engine start, taxi, and takeoff checks were all completed in accordance with the checklists with no anomalies noted. The pilot/owner reported that during the takeoff roll, the airplane seemed to 'take forever” to reach takeoff speed and that it used 'the whole runway.” When the airplane reached about 1,000 feet mean sea level, the engine stopped producing power, and the instructor took control of the airplane. He turned the airplane back toward the departure airport and performed remedial actions to regain engine power but was unsuccessful. When he determined the airplane would not reach the airport, he performed a forced landing to wooded terrain. The airplane sustained substantial damage to the wings, fuselage, and empennage. Both pilots egressed without assistance. Examination of the wreckage revealed no preimpact mechanical malfunctions or failures that would have precluded normal operation. Examination of the fuel system found it intact. Removal of the fuel pump caused water to spill from the pump. The pump was actuated by hand, and water was ejected from the pump. The carburetor float bowl contained a '50-50” mixture of water and fuel. The water in the fuel system, which should have been detected during a preflight inspection, led to the loss of engine power during takeoff.

Probable Cause: A total loss of engine power due to water contamination of the fuel. Contributing to the accident was the pilot/owner's inadequate preflight inspection.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA12LA397
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB ERA12LA397

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 13:19 ASN Update Bot Added

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