Fuel exhaustion Accident Air Tractor AT-602 N51037,
ASN logo
ASN Wikibase Occurrence # 287803
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Monday 9 April 2012
Time:12:30 LT
Type:Silhouette image of generic AT6T model; specific model in this crash may look slightly different    
Air Tractor AT-602
Owner/operator:Boyle Flying Service Inc
Registration: N51037
MSN: 602-0464
Year of manufacture:1997
Total airframe hrs:5311 hours
Engine model:P&W Canada PT6A-66 SER
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Ruleville, Mississippi -   United States of America
Phase: Standing
Nature:Agricultural
Departure airport:Boyle, MS
Destination airport:Boyle, MS
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot departed on an aerial application flight with an estimated 53 gallons of fuel. He had not reset the fuel totalizer before departure. He made numerous passes over a 100-acre field spraying fertilizer during the 30 minute flight. After his last pass, the pilot noticed a fuel flow fluctuation. The engine subsequently lost power at an altitude of 75 to 100 feet above the ground, and the pilot made a forced landing. He pulled the airplane off the ground again briefly to clear an obstruction; however, when the airplane touched down again, the left main landing gear sank into soft ground and sheared off. The airplane rotated to the right onto its nose, and the left wing sustained structural damage. Postaccident examination revealed that the left and right main fuel caps had a tight seal and there was no evidence of streaking or venting of fuel on the airplane or on the ground. The left, right, header, and purge fuel tanks were drained and yielded about 34 total ounces of fuel—two ounces from the right fuel tank and 32 ounces from the header tank. The left and purge tanks contained no fuel. No preaccident mechanical malfunctions or failures were found that would have precluded normal operation.

Probable Cause: The pilot's inadequate preflight planning and in-flight fuel management, which resulted in a total loss of engine power due to fuel exhaustion.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA12CA275
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB ERA12CA275

History of this aircraft

Other occurrences involving this aircraft
9 April 2010 N51037 Boyle Flying Service, Inc 0 Ruleville, MS sub
4 June 2021 N51037 Boyle Flying Service Inc 0 Drew, Mississippi sub

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 14:36 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org