Accident Cessna 177RG N33224,
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ASN Wikibase Occurrence # 287957
 
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Date:Thursday 28 October 2010
Time:09:45 LT
Type:Silhouette image of generic C77R model; specific model in this crash may look slightly different    
Cessna 177RG
Owner/operator:Panama City Beach Flying Club LLC
Registration: N33224
MSN: 177RG0928
Total airframe hrs:7216 hours
Engine model:Lycoming IO-360-A1B6D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Bedford, Kentucky -   United States of America
Phase: En route
Nature:Private
Departure airport:Richmond Airport, IN (RID/KRID)
Destination airport:Shelbyville-Bomar Field, TN (SYI/KSYI)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that he filled the airplane's fuel tanks with full fuel prior to departing on the cross-country flight. Approximately 30 minutes into the flight, at an altitude of 3,000 feet above ground level, the engine suddenly stopped producing power. The pilot checked the fuel mixture and fuel selector settings and attempted to restore engine power but was unsuccessful. He maneuvered the airplane for a forced landing in a field and landed with the gear in the retracted position, resulting in substantial damage to the airplane's fuselage. Postaccident examination of the engine compartment by a Federal Aviation Administration (FAA) inspector revealed that the flexible fuel hose that connects to the inlet fitting of the servo fuel injector was separated from the inlet fitting. No damage to any portion of the fitting or to the B-nut, or to the threads of the fitting or B-nut was noted, and there was no evidence of torque seal putty on the B-nut. There was no provision for safety wire to secure the B-nut. The most recent annual inspection was performed approximately 7 flight hours since the inspection. The mechanic who performed the annual inspection stated to an FAA inspector that he did remove the separated line during the inspection to gain access to the fuel inlet screen. He further stated that about the time of the inspection he incorporated a process of applying purple colored torque seal putty on components that he disassembled or removed.

Probable Cause: The mechanic's failure to properly secure a fuel line when it was reinstalled during an engine inspection.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA11CA047
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB ERA11CA047

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 17:06 ASN Update Bot Added

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