ASN Wikibase Occurrence # 287967
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 21 October 2010 |
Time: | 18:15 LT |
Type: | Rockwell Commander 112TC |
Owner/operator: | Kalunji Aviation Group, LLC |
Registration: | N1154J |
MSN: | 13091 |
Year of manufacture: | 1976 |
Total airframe hrs: | 1890 hours |
Engine model: | Lycoming IO-360-C1A6D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Waynesboro, Georgia -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Covington, GA (9A1) |
Destination airport: | Columbia-Owens Field, SC (CUB/KCUB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot completed several touch-and-go takeoffs and landings at his home airport before departing on a cross-country flight. While in cruise flight, he declared an emergency due to a lack of elevator and aileron control. He attempted to troubleshoot the problem over the radio with air traffic controllers and other pilots on his assigned frequency. The pilot made multiple approaches but could not complete the landing before he began to run out of daylight and his fuel state became critical. He maneuvered the airplane south of the airport toward a wooded area away from homes. About 1,500 feet above ground level, the airplane's fuel supply was exhausted, the engine stopped producing power, and the pilot parachuted from the airplane, using a recently purchased parachute that he had brought on board. The airplane departed controlled flight and descended to the ground; the pilot suffered no injuries.
Four days prior to the accident, the accident pilot appeared at a parachute school with an emergency parachute rig and asked the owner/instructor of the school to teach him how to deploy the parachute. According to the owner/instructor, when he asked the pilot why he needed an emergency parachute, the pilot stated he was a pilot flying out of a nearby Air Force base and that he flew L-39 jets, acting as the 'rabbit†for Marine pilots to chase him in dog-fight training. The instructor thought it was strange that the pilot had not gone to jump school, and the pilot stated it was not required. He added that the airplanes he was flying for the Marines did not have ejection seats, and if he needed to get out, he would have to climb out.
A detailed examination of the airplane revealed no evidence of any binding or restriction of movement of the elevator or elevator trim surfaces, no evidence of cable interference from foreign objects, no evidence of any binding or restriction of movement of the internal pulleys or cables, and the cables, turnbuckles, and cable pulleys were in good condition and moved freely. Examination of the instruments mounted in the instrument panel revealed that the serial numbers on the air pressure instruments matched the serial numbers of the air pressure instruments that the pilot/owner reported stolen in July 2010.
Probable Cause: The pilot's deliberate exiting of the airplane by parachute while in flight following a reported flight control malfunction that could not be verified.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA11LA033 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB ERA11LA033
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 17:13 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation