Loss of control Accident Cessna 180 N2576K,
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ASN Wikibase Occurrence # 287978
 
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Date:Sunday 17 October 2010
Time:08:30 LT
Type:Silhouette image of generic C180 model; specific model in this crash may look slightly different    
Cessna 180
Owner/operator:Clinton Goodhue
Registration: N2576K
MSN: 18052998
Year of manufacture:1978
Total airframe hrs:3035 hours
Engine model:Continental O470
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Summner, Maine -   United States of America
Phase: Landing
Nature:Private
Departure airport:Sidney, ME
Destination airport:Summner, ME
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, while the airplane was on final approach at the destination airport, it encountered a downdraft and he was unable to arrest the descent rate, even with full power. A witness stated that the wind at the airport at the time of the accident was 8-10 knots. The nearest weather reporting station also reported that the wind was from 360 degrees at 6 knots. Another witness also reported that the pilot of the accident airplane would usually approach at a slow approach speed for landing. Review of a video recording that was made at the airport on the day of the accident also confirmed that there was little or no wind present during the accident, and that the airplane appeared to approach the runway at a slower airspeed than similar airplanes. Further review of the video also revealed that, while on short final, the airplane had developed a high sink rate and rapidly rolled to the right just prior to impact with the turf runway. No sound of an increase of engine power was recorded until just prior to ground contact. During an interview, the pilot stated there were no mechanical malfunctions with the airplane. Examination of the airplane by a Federal Aviation Administration inspector revealed that during the accident the airplane incurred substantial structural damage to the landing gear assembly bulkhead.

Probable Cause: The pilot's failure to maintain adequate airspeed while on final approach resulting in an aerodynamic stall and a subsequent hard landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA11CA024
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB ERA11CA024

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 17:19 ASN Update Bot Added

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