Gear-up landing Accident Piper PA-46-310P Malibu N24WW,
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ASN Wikibase Occurrence # 288081
 
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Date:Sunday 12 September 2010
Time:11:04 LT
Type:Silhouette image of generic PA46 model; specific model in this crash may look slightly different    
Piper PA-46-310P Malibu
Owner/operator:Avionta LLC
Registration: N24WW
MSN: 46-8508071
Year of manufacture:1985
Total airframe hrs:4713 hours
Engine model:Continental TSIO 520 Seri
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Farmington, New Mexico -   United States of America
Phase: Approach
Nature:Executive
Departure airport:Durango, CO (00C)
Destination airport:Farmington, NM
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was landing after completing a practice instrument landing system approach in bright day conditions. The pilot reported that he extended the landing gear and flaps when he was about three miles from the airport. The airplane crossed the threshold of the runway and was just about to touch down when the pilot noticed that the landing gear green indicator lights appeared not to be illuminated. The pilot applied full throttle and immediately raised the landing gear and flaps. During the go-around attempt the airplane settled and the propeller struck the runway. The pilot held full power and a nose-high attitude as the airspeed decreased. The airplane struck obstructions on the side of the runway, resulting in substantial damage to the left wing. It then came to rest upright approximately halfway down the length of the runway. An inspection of the aircraft systems by a Federal Aviation Administration inspector revealed that the cockpit lighting dimmer switch, which controlled the illumination intensity of the landing gear lights, was set to the 'Night Dim” position.

Probable Cause: The pilot's premature retraction of the landing gear and the flaps during landing. Contributing to the accident was the inadvertent dimming of the cockpit lighting, resulting in a perceived unsafe gear configuration.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN10CA533
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB CEN10CA533

History of this aircraft

Other occurrences involving this aircraft
19 March 1993 N24WW Private 0 Hailey, ID sub

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 18:20 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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