ASN Wikibase Occurrence # 288361
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 5 July 2010 |
Time: | 13:00 LT |
Type: | Cessna 182M Skylane |
Owner/operator: | White Sands Soaring Assoc Inc |
Registration: | N71784 |
MSN: | 18259755 |
Year of manufacture: | 1969 |
Engine model: | Continental O-470 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Alamagordo, New Mexico -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Alamogordo Municipal Airport, NM (ALM/KALM) |
Destination airport: | Alamogordo Municipal Airport, NM (ALM/KALM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was returning to land after towing a glider to altitude. The wind was gusting up to 19 knots and shifting. The pilot made two attempts to land, but elected to go around each time due to a shimmy in the main landing gear. On the third attempt to land he switched to another runway, composed of dirt. During the landing, the airplane bounced and he elected to go around. Convinced that was something wrong with the landing gear, the pilot performed a low approach over the runway and asked ground personnel to visually check the landing gear; they verified that it looked normal. The pilot made another attempt to land and, during touchdown, the airplane bounced hard 2 to 3 times. Again, the pilot elected to go around and decided to try another landing on the original runway. After landing, the landing gear continued to shimmy and the airplane veered toward the right side of the runway. As the plane slowed, the pilot was able to taxi the airplane safely back to the ramp. A postaccident examination of the airplane revealed that the firewall was wrinkled, the engine mounts were deformed, and the fuselage was damaged at the waterline. Flight control continuity was confirmed and no anomalies were found with the engine or other airplane systems.
Probable Cause: The pilot's loss of airplane control during landing, which resulted in a hard/bounced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN10LA383 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB CEN10LA383
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 21:39 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation