Hard landing Accident Seawind 3000 N79DJ,
ASN logo
ASN Wikibase Occurrence # 288408
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Wednesday 23 June 2010
Time:13:25 LT
Type:Silhouette image of generic SEAW model; specific model in this crash may look slightly different    
Seawind 3000
Owner/operator:private
Registration: N79DJ
MSN: 48
Year of manufacture:2010
Total airframe hrs:43 hours
Engine model:Lycoming IO-540-EXP
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Sanibel Island, Florida -   United States of America
Phase: En route
Nature:Private
Departure airport:Key West International Airport, FL (EYW/KEYW)
Destination airport:Sarasota-Bradenton Airport, FL (SRQ/KSRQ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot of the experimental, amateur-build amphibian airplane was also the owner/builder. While descending through 6,000 feet mean sea level, a vibration developed in the elevator control. The pilot reduced engine power and the vibration decreased. When the pilot increased engine power, the vibration increased and he had to reduce engine power to a point where the airplane could not maintain altitude. The pilot subsequently performed a forced landing to water. The airplane touched down hard, which resulted in damage to the engine nacelle and empennage. A postaccident examination of the airplane revealed that approximately three-fourths of the elevator had separated in-flight. Metallurgical examination revealed that the elevator failed due to overstress, in the downward direction.

The pilot completed construction of the airplane about 3 weeks prior to the accident and the airplane had accrued 43 total hours of operation since its completion. The airplane was equipped with an empennage manufactured by a different manufacturer than that of the kit manufacturer, which was 49 percent larger than the kit empennage. Although the increased size did not add much weight, it added significant surface area, resulting in increased gust loads, with no added engineering to compensate for such loads.

The airplane's never exceed speed (Vne) was 230 mph (200 knots) and the maneuvering speed (Va) was 180 mph (156 knots). Review of a radar plot for the accident flight, overlaid on weather radar data, revealed that the accident airplane was traveling at a groundspeed of approximately 200 knots, in the vicinity of convective activity.

Probable Cause: An overstress failure of the elevator. Contributing to the accident was the owner/builder's modification of the experimental airplane beyond the recommendations of the kit manufacturer.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA10LA328
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB ERA10LA328

History of this aircraft

Other occurrences involving this aircraft
18 February 2021 N79DJ Private 0 Venice Municipal Airport (VNC/KVNC), Venice, FL unk
Gear-up landing

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 22:05 ASN Update Bot Added
15-Sep-2023 19:10 harro Updated

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org