Accident Eurocopter AS 350 B3 N4282,
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ASN Wikibase Occurrence # 288661
 
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Date:Tuesday 16 March 2010
Time:08:30 LT
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different    
Eurocopter AS 350 B3
Owner/operator:Omniflight Helicopters Inc.
Registration: N4282
MSN: 4282
Year of manufacture:2007
Total airframe hrs:819 hours
Engine model:Turbomeca ARRIEL 2B1
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Parker, Arizona -   United States of America
Phase: Standing
Nature:Unknown
Departure airport:Parker, AZ (AZ47)
Destination airport:Parker, AZ (AZ47)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot of the helicopter told the lead mechanic that the main rotor blade needed to be balanced. Two mechanics showed up on the morning of the accident and installed the balancing equipment. A test flight was flown. The two men performed the necessary work, which required a second adjustable wrench on the top of the rotor head to hold the bolt while the nut below was removed and later torqued back on. When the work was finished, the men gathered their tools. The pilot asked the lead mechanic if they had gathered all their tools and the mechanic replied "yes." The three men got on the helicopter for a test hover to check their work. As the main rotor speed reach 100 percent, the three occupants heard a "bang." As the helicopter hovered, the two mechanics thought the balancing equipment readings were worse than the first flight, and the vibrations in the aircraft had increased. The pilot landed the helicopter so that the mechanics could make additional adjustments. The mechanics discovered that they were missing the adjustable wrench that had been used on the top of the main rotor head. Postaccident examination revealed that one main rotor blade, the tail boom, and the lower vertical stabilizer had received damage from the unaccounted for wrench.

Probable Cause: The mechanics' failure to account for all the tools following a maintenance procedure and the pilot's failure to perform a preflight check before a maintenance test flight.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR10CA164
Status: Investigation completed
Duration: 3 months
Download report: Final report

Sources:

NTSB WPR10CA164

Location

Revision history:

Date/timeContributorUpdates
05-Oct-2022 00:55 ASN Update Bot Added

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