ASN Wikibase Occurrence # 288701
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 23 February 2010 |
Time: | 15:45 LT |
Type: | Diamond DA20-C1 |
Owner/operator: | Utah Valley University |
Registration: | N894CT |
MSN: | C0094 |
Total airframe hrs: | 6054 hours |
Engine model: | Continental IO-240 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Delta, Utah -
United States of America
|
Phase: | Approach |
Nature: | Training |
Departure airport: | Provo Airport, UT (PVU/KPVU) |
Destination airport: | Delta Airport, UT (DTA/KDTA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The student pilot was on his first solo cross-county fight, which had as its planned destination an airport that he had never been to prior to that flight. Upon arriving at the unfamiliar airport, he overflew the area in order to get a sight picture of the situation. He then flew a non-standard pattern to the final approach of the runway he chose to land on. Although his approach had not become stabilized by short final, he decided to continue the landing. When the airplane's main gear contacted the runway, it bounced back into the air, and the pilot decided to execute a go-around. During the go-around, the pilot, who said the engine sounded like it went to full rpm, did not let the airplane stabilize and accelerate before retracting the flaps, and he therefore found that the airplane would not maintain the climb that he tried to establish. As he attempted to continue the go-around, the airplane slowed and its left wing dropped, and the pilot was unable to maintain directional control. The airplane then descended into the soft terrain off the left side of the runway, and nosed over onto its back. The airplane sustained substantial damage to its wings, fuselage, and empennage. A Federal Aviation Administration inspector monitored an engine inspection and test run, which did not reveal any anomalies or issues with the engine, which was able to be run to full power.
Probable Cause: The student pilot's incorrect use of the flaps and failure to attain and maintain an adequate airspeed during the attempted go-around procedure, which led to a stall/mush condition. Contributing to the accident was the student pilot's lack of familiarity with the destination airport, and his delayed decision to execute the go-around.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10CA146 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB WPR10CA146
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 01:20 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation