ASN Wikibase Occurrence # 288757
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Date: | Friday 18 November 2011 |
Time: | 16:00 LT |
Type: | Stinson 108-1 |
Owner/operator: | |
Registration: | N9016K |
MSN: | 108-2016 |
Engine model: | Franklin 6A4150 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Boulder City, Nevada -
United States of America
|
Phase: | Taxi |
Nature: | Private |
Departure airport: | Cedar City Airport, UT (CDC/KCDC) |
Destination airport: | Boulder City Municipal Airport, NV (BLD/KBVU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he landed with a gusting crosswind of 18 to 27 knots. At the end of the runway he made a 180 degree turn to back-taxi to the intersection for the ramp. During the back-taxi, the airplane veered to the right. The pilot applied the left brake, but it did not have enough braking action to stop the turn. The pilot also applied left rudder control and increased power for more rudder authority, but the airplane subsequently departed the runway pavement. The right main gear leg folded under the fuselage, the nose dug into the dirt breaking the wooden propeller, and the right wing tip contacted the ground. Postaccident examination of both the left and right brake systems revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. Fluid was found in both master cylinder reservoirs. Pedal pressure was even, firm, and normal. When brake pedal pressure was applied, both left and right calipers compressed against the rotors and released normally. Given the gusting crosswind, the wind likely led to the pilot's loss of directional control.
Probable Cause: The pilot's failure to maintain directional control while taxiing with a gusting crosswind.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR12LA045 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB WPR12LA045
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 04:30 |
ASN Update Bot |
Added |
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