ASN Wikibase Occurrence # 288820
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Date: | Wednesday 5 October 2011 |
Time: | 16:00 LT |
Type: | Cessna 180J |
Owner/operator: | Private |
Registration: | N180RN |
MSN: | 18052561 |
Year of manufacture: | 1975 |
Total airframe hrs: | 3498 hours |
Engine model: | Continental O-470S |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Norfolk, Virginia -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Norfolk-Hampton Roads Executive Airport, VA (KPVG) |
Destination airport: | Elizabeth City Airport, NC (ECG/KECG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that, as he started to taxi onto the runway, the airplane was difficult to turn. He thought that the tailwheel had not locked into position so he lined up on the center line of the runway and pulled forward to give the tailwheel time to lock into position. He then initiated the takeoff roll and lifted the tail as the airspeed increased. The airplane then pulled to the left, and the pilot applied right rudder, but the left main landing gear went off the left side of the runway. He immediately applied the brakes and reduced power to abort the takeoff; however, the airplane turned 90 degrees, struck a ditch, and the right main landing gear separated from the airplane. A postaccident examination of the brake system revealed no anomalies; however, the brakes could not be tested because the hydraulic system was breached. A nut was found separated from a right main landing gear attach bolt after the accident, but the investigation was unable to determine if the separated nut contributed to the airplane veering to the left during takeoff.
Probable Cause: The pilot's inability to maintain directional control during takeoff for undetermined reasons. Contributing to the accident was the pilot's delayed decision to abort the takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA016 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB ERA12LA016
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 06:33 |
ASN Update Bot |
Added |
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