Runway excursion Accident Van's RV-6A N241BD,
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ASN Wikibase Occurrence # 288883
 
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Date:Saturday 3 September 2011
Time:07:47 LT
Type:Silhouette image of generic RV6 model; specific model in this crash may look slightly different    
Van's RV-6A
Owner/operator:
Registration: N241BD
MSN: 60477
Total airframe hrs:1555 hours
Engine model:Lycoming O&VO-360 SER
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Hollywood, Florida -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Hollywood-North Perry Airport, FL (HWO/KHWO)
Destination airport:Palatka, FL (28J)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During the airplane's initial climb after takeoff, when it was an estimated 30 to 50 feet off the ground, the propeller rpm suddenly decreased. The pilot aborted the takeoff, and was able to land the airplane about 500 feet before the end of the 3,350-foot runway. However, the airplane then overran the runway end and impacted a perimeter fence. Initial examination of the engine did not reveal any anomalies, but a subsequent propeller governor disassembly at a propeller shop revealed difficulty in moving an internal part, as well as internal scoring internal scoring. Further examination of the cleaned parts confirmed the internal scoring as well as internal chipping, the latter which was likely produced by trapped particles. Chipping was found on the land (surface) of the pilot valve, and rounding on the edge of the port it normally interacted with, which would produce erratic operation of the governor, and therefore affect propeller speed. Because the parts had previously been cleaned, there were no particulates available for composition analysis. However, because there was also no evidence of missing material from the governor itself, it was likely that the damage to the governor was the result of particulate ingestion via oil flow from the engine.

Probable Cause: Particulate ingestion from the engine, which resulted in the malfunction of the propeller governor during the airplane's initial climb.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA11LA483
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB ERA11LA483

History of this aircraft

Other occurrences involving this aircraft
2 September 2016 N241BD Private 2 Turner County, 10mi W of Viborg, SD w/o

Location

Revision history:

Date/timeContributorUpdates
05-Oct-2022 07:15 ASN Update Bot Added

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