ASN Wikibase Occurrence # 288996
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Date: | Friday 5 August 2011 |
Time: | 16:42 LT |
Type: | Cessna T210N |
Owner/operator: | Muy Flying LLC |
Registration: | N829MB |
MSN: | 21063116 |
Year of manufacture: | 1978 |
Total airframe hrs: | 5454 hours |
Engine model: | Continental TSIO-520 SER |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Amarillo, Texas -
United States of America
|
Phase: | Approach |
Nature: | Executive |
Departure airport: | Dumas-Moore County Airport, TX (KDUX) |
Destination airport: | Amarillo-Rick Husband International Airport, TX (AMA/KAMA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot noticed a loss of engine power while descending to land, and he made several unsuccessful attempts to restart the engine. The pilot was unable to maintain altitude and made a forced landing to rugged, uneven terrain north of the runway. During the landing roll, the airplane struck a gully and flipped over. The pilot said he did not observe any fuel leaking from the airplane after the accident, and a postaccident inspection of the grassy area around and under the airplane revealed no discoloration from fuel exposure. Examination of the fuel system revealed no mechanical anomalies or blockages, and the fuel selector was set to the right fuel tank. A review of fuel receipts and data downloaded from the engine analyzer revealed there should have been about 58 gallons of fuel on board at the time of the accident. However, only 20 gallons of fuel (15 gallons from the right tank and 5 gallons from the left tank) were drained from the airplane. The missing 38 gallons could not be accounted for.
Data from the engine analyzer was downloaded and confirmed a loss of engine power, but it did not identify the cause of the loss of engine power. About 1 minute later, both values dropped to zero. When the engine was test run, it started immediately and ran through its full power band without interruption. No mechanical anomalies were noted that would have precluded the engine from operating normally. Even with a discrepancy of 38 gallons, there was still adequate fuel available for the engine to continue operating. It could not be determined what caused the loss of engine power.
Probable Cause: A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN11LA552 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB CEN11LA552
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 08:37 |
ASN Update Bot |
Added |
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