Loss of control Accident Tl Ultralight Sro STING S3 N2442,
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ASN Wikibase Occurrence # 289041
 
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Date:Friday 29 July 2011
Time:11:47 LT
Type:Silhouette image of generic TL20 model; specific model in this crash may look slightly different    
Tl Ultralight Sro STING S3
Owner/operator:Universal Flight Training, LLC
Registration: N2442
MSN: TLUSA174
Total airframe hrs:179 hours
Engine model:Rotax 912ULS
Fatalities:Fatalities: / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Sarasota, Florida -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Training
Departure airport:Sarasota, FL
Destination airport:Sarasota, FL
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The purpose of the flight was a demonstration flight for the pilot-rated student who had not flown in 16 years. The pilot-in-command (PIC) seated in the right seat stated that he performed weight and balance calculations before departure and based his calculations on the provided passenger weight (275 pounds); reporting the airplane was at the top of the envelope but within weight and balance.

The PIC elected to depart with the aircraft parachute system activation handle safety pin installed because as he later stated he had not been trained on its use, and because he did not intend on flying above 3,000 feet. After departure the flight climbed to between 2,300 and 2,400 feet, where a stall was performed and the flight entered a spin. The airplane descended uncontrolled into a large tree then impacted the ground coming to rest upright. The left seat occupant advised the 911 dispatcher while summoning assistance that the PIC was unable to recover from the spin. Both occupants were airlifted to a hospital where the left seat occupant died while hospitalized 3 days later. The PIC reported the next day while hospitalized he could not recall how or why the airplane entered a spin.

Postaccident inspection of the airplane following recovery revealed no evidence of preimpact failure or malfunction of the aileron, elevator, or rudder flight control systems. The flaps were found fully extended, and there was no preimpact failure or malfunction of the primary or secondary flight controls, or of the structure necessary to sustain flight. Inspection of the engine-driven fuel pump revealed superficial cracks on the dry side of the diaphragm of the engine-driven fuel pump, which initial testing revealed it incapable of sustaining engine operation but subsequent testing revealed it did allow engine operation; the auxiliary fuel pump tested satisfactory. No other discrepancies were identified during the engine examination. While the airplane was equipped with a ballistic recovery system parachute, the safety pin was not removed which contradicted the procedures in the Pilot Operating Handbook. Further, the location of the activation handle behind the co-pilot's seat rendered it difficult to access for the pilot-in-command seated in the right seat during the uncontrolled descent.

While the left seat occupant indicated with the operator that his weight was 275 pounds, which was the same amount listed on his last FAA medical application from December 1989; the external examination indicated he weighed 340 pounds. The weight he did provide was 25 pounds in excess of the maximum weight allowed for the seat determined during design and testing. Further, the weight determined during the external examination resulted in the airplane being 64 pounds above maximum ramp weight at engine start. Although the left seat outboard attach structure separated during the impact sequence, that condition was attributed to the exceedance of the maximum allowed seat weight by 90 pounds.

Although the airplane had been spin tested by the manufacturer, it was not approved for intentional spins. No determination could be made as to why the PIC was unable to recover from the inadvertent spin.

Probable Cause: The inability of the pilot-in-command (PIC) to recover from an inadvertent spin following a stall demonstration for reasons that could not be determined because aircraft and engine examinations did not reveal any anomalies that would have precluded recovery from the spin. Contributing to the severity of the accident were the PIC's failure to remove the airframe parachute system safety pin before takeoff, the exceedance of the left-seat weight limitation, and the location of the parachute system activation handle behind the PIC's seat, which prevented easy access during the uncontrolled descent.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA11LA427
Status: Investigation completed
Duration: 2 years and 4 months
Download report: Final report

Sources:

NTSB ERA11LA427

Location

Revision history:

Date/timeContributorUpdates
05-Oct-2022 09:06 ASN Update Bot Added

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