Accident Ryan Navion A N4911K,
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ASN Wikibase Occurrence # 289060
 
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Date:Sunday 24 July 2011
Time:17:40 LT
Type:Silhouette image of generic NAVI model; specific model in this crash may look slightly different    
Ryan Navion A
Owner/operator:Liddle Cable Co Inc
Registration: N4911K
MSN: NAV-4-1911
Total airframe hrs:5371 hours
Engine model:Continental O-470-13
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Torrington, Wyoming -   United States of America
Phase: Approach
Nature:Private
Departure airport:North Platte-Lee Bird Field, NE (LBF/KLBF)
Destination airport:Torrington Municipal Airport, WY (TOR/KTOR)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he leaned the mixture while en route, but could not find the peak performance. He set the mixture control to what he thought it was appropriate for 5,000 to 6,000 feet altitude. As he entered the landing pattern at his destination, he lowered the landing gear and prepared for landing. As he reduced the throttle position, the engine lost all power, and the descent rate increased. The pilot determined that the airplane would not glide to a runway and maneuvered to an open area. The airplane touched down hard, and the landing gear collapsed. The airplane sustained substantial damage to the firewall and fuselage. Postaccident examination of the airframe and engine revealed no mechanical malfunctions or failures that would have precluded normal operation. The carburetor was removed and connected to a test cell. The unit was found out of limits at the low end of its operating range. Thus, with the fuel mixture leaned and a subsequent reduction in the power for landing, a temporary disruption of the fuel flow caused the engine to sputter and lose power.

Probable Cause: The carburetor's failure to meet its operating limits at the low range, which resulted in a loss of engine power when the pilot reduced power for landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR11LA346
Status: Investigation completed
Duration: 2 years and 8 months
Download report: Final report

Sources:

NTSB WPR11LA346

Location

Revision history:

Date/timeContributorUpdates
05-Oct-2022 09:18 ASN Update Bot Added

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