ASN Wikibase Occurrence # 289191
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Date: | Thursday 23 June 2011 |
Time: | 11:55 LT |
Type: | Enstrom F-28C-2 |
Owner/operator: | P And N Corporation |
Registration: | N5694A |
MSN: | 491-2 |
Year of manufacture: | 1980 |
Total airframe hrs: | 3706 hours |
Engine model: | Lycoming HIO-360-E1AD |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Blair, Nebraska -
United States of America
|
Phase: | Standing |
Nature: | Survey |
Departure airport: | Plattsmouth Municipal Airport, NE (KPMV) |
Destination airport: | Blair, NE |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting an aerial observation flight in a helicopter when he felt a high vibration in the tail rotor system in conjunction with a sharp jerk in the anti-torque pedals. The pilot autorotated to a wet field and the helicopter subsequently rolled over. A postaccident examination of the helicopter revealed that a pitch link retaining bolt had come loose from the pitch link attachment horn. The bolt and its associated hardware separated in flight and the bolt hole where the pitch link attached was elongated. According to the helicopter's preflight inspection checklist, the pitch link should have been checked before flight for binding or looseness; however, the pilot could not recall if he actually checked it. The helicopter underwent a 100-hour maintenance inspection two weeks before the accident. At that time, the maintenance manual required an inspection in which the pitch links would have to be disconnected then reassembled. Since the pitch link retaining bolt and its associated hardware were never recovered, it could not be determined if the pitch link assembly had been properly installed or torqued at the last inspection. The pitch link failure occurred about 14 hours after this inspection. The Federal Aviation Administration reported that they were not aware of any instances prior to this accident where the tail rotor pitch link assemblies became loose and failed prematurely after proper installation.
Probable Cause: The failure of a tail rotor pitch change link due to the retaining bolt becoming separated in flight. Contributing to the accident was the pilot's inadequate preflight inspection.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN11LA414 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB CEN11LA414
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 10:52 |
ASN Update Bot |
Added |
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