ASN Wikibase Occurrence # 289207
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Date: | Saturday 18 June 2011 |
Time: | 17:45 LT |
Type: | Bell 47G-4A |
Owner/operator: | Rhineland Grain Inc |
Registration: | N24HM |
MSN: | 7688 |
Year of manufacture: | 1970 |
Total airframe hrs: | 11153 hours |
Engine model: | Lycoming VO-540 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Montgomery City, Missouri -
United States of America
|
Phase: | Landing |
Nature: | Agricultural |
Departure airport: | Montgomery City, MO (PVT |
Destination airport: | Montgomery City, MO (PVT |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he had returned from an agricultural application to reload the cleaning solution. Unbeknownst to the pilot, the helicopter was loaded with approximately 90 gallons of solution, instead of the expected 70 gallons for the flight.
The pilot reported that he increased engine power and lifted off; however, immediately after lift off the engine and rotor speed began to decrease. He selected a suitable landing point and flared for touchdown about 10 feet above ground level to minimize the forward speed. The helicopter touched down on the rear portion of the landing skids and began to pitch forward. He applied aft cyclic control to prevent the helicopter from nosing over. He subsequently heard a bang and observed debris coming from the aircraft. He shut down the engine and secured the helicopter.
A postaccident examination revealed that the main rotor had struck the tailboom resulting in substantial damage to the airframe. The pilot said the helicopter may have been on a slight incline when the solution was loaded, allowing the right side tank to fill more than the left side tank. He was unaware of the overload condition. The pilot added that closer monitoring of the helicopter and chemical truck incline, and the final amount of solution being loaded onto the helicopter, might have prevented the accident. The pilot did not report any failures or malfunctions that would have precluded normal operation.
Probable Cause: A loss of control during the precautionary landing, which resulted in inadvertent contact between the main rotor and the tailboom. Contributing to the accident was the overloaded condition.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN11CA403 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB CEN11CA403
History of this aircraft
Other occurrences involving this aircraft
24 July 2008 |
N24HM |
Reabe Flying Service |
|
Mayville, Wisconsin |
|
min |
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 11:04 |
ASN Update Bot |
Added |
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