ASN Wikibase Occurrence # 289393
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Date: | Wednesday 13 April 2011 |
Time: | 17:55 LT |
Type: | Cessna 172S |
Owner/operator: | Bay Air Flying Service |
Registration: | N2468Z |
MSN: | 172S10065 |
Year of manufacture: | 2005 |
Total airframe hrs: | 2441 hours |
Engine model: | Lycoming IO-360-L2A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Saint Petersburg, Florida -
United States of America
|
Phase: | Take off |
Nature: | Training |
Departure airport: | St Petersburg-Albert Whitted Airport, FL (KSPG) |
Destination airport: | St Petersburg-Albert Whitted Airport, FL (KSPG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The student pilot stated that after takeoff during his second supervised solo flight, he remained in the traffic pattern and landed uneventfully. During the landing roll he elected to perform a touch-and-go landing and applied power for takeoff. Immediately after adding power, the airplane turned left. He applied right rudder to correct the left turn but then decided to perform a full stop landing. He applied the brakes in an effort to keep the airplane on the runway, and reduced power before the airplane departed the runway, and went into water while traveling about 30 knots. The student pilot reported no preimpact mechanical malfunctions or failures with the airplane that would have precluded normal operation. The student's certified flight instructor stated that after veering to the left, the airplane exited the runway, crossed a perpendicular runway, and then impacted a ditch at which time he heard power applied. He then observed the airplane travel into the water and ran to the airplane to assist his student. Postaccident inspection of the flight controls revealed no evidence of preimpact failure or malfunction. The airplane sustained substantial damage to the firewall and fuselage.
Probable Cause: The failure of the student pilot to maintain directional control during a touch-and-go landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA11CA244 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB ERA11CA244
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 13:13 |
ASN Update Bot |
Added |
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