ASN Wikibase Occurrence # 289478
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Date: | Tuesday 15 March 2011 |
Time: | 12:30 LT |
Type: | Cessna 182P Skylane |
Owner/operator: | Armstrong Equipment Leasing Co |
Registration: | N430ML |
MSN: | 18263045 |
Year of manufacture: | 1974 |
Total airframe hrs: | 5050 hours |
Engine model: | Continental IO-550 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Alachua, Florida -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Leesburg International Airport, FL (LEE/KLEE) |
Destination airport: | Lake City, FL (15FL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While the pilot was maneuvering the airplane to set up a visual approach, the engine lost partial power. The pilot attempted to restore full engine power but was unsuccessful. Subsequently, he made a forced landing in a field, and the airplane nosed over. A postaccident examination of the engine revealed that it would only partially rotate by hand with resistance. Further examination revealed that the camshaft gear was missing nine teeth and that one tooth was damaged. The crankshaft gear was missing four consecutive teeth, and one tooth was missing from another location on the gear. A metallurgical evaluation of the camshaft gear, crankshaft gear, an exhaust valve, and a lifter revealed that the components met all the material properties requirements. The fracture surfaces on the camshaft and crankshaft gears were damaged due to post-separation contact. Debris from the oil sump was identified as nitrided gear material and lifter fragments. The engine had accumulated about 12 hours of operating time since its most recent inspection, which included an oil change. At the time of the accident, the engine had accumulated a total time of 750.7 hours. According to the owner and the engine maintenance log, no propeller strikes had occurred since the engine was installed on the airframe.
Probable Cause: A loss of engine power due to the failure of the camshaft gear teeth and crankshaft gear teeth for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA11LA190 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB ERA11LA190
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 14:18 |
ASN Update Bot |
Added |
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