ASN Wikibase Occurrence # 289557
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Date: | Saturday 5 February 2011 |
Time: | 17:51 LT |
Type: | Cessna 150L |
Owner/operator: | Michael Schaff |
Registration: | N11790 |
MSN: | 15075634 |
Year of manufacture: | 1974 |
Engine model: | Continental 0-200 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gonzales, Louisiana -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | Baton Rouge Metropolitan Airport, LA (BTR/KBTR) |
Destination airport: | Gonzales, LA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The certified flight instructor did not visually inspect the fuel tanks prior to departure, but noted that the fuel gauge was just below the full mark, and the student pilot told him the fuel tanks were full. Based on his experience in the airplane, the instructor estimated a total of 4 hours of fuel on board and then departed on an instructional flight that included numerous practice take offs and landings. Approximately 3 hours into the flight, as they were returning to their home airport, the engine lost power. The instructor was unable to re-start the engine and made a forced landing to a grass field where the right wing impacted a tree, resulting in substantial damage to the strut. A Federal Aviation Administration inspector drained both fuel tanks and reported that approximately 3/4 of a gallon of fuel was drained from the right wing tank and 1/2 of a gallon of fuel was drained from the left wing tank. The fuel line to the carburetor was removed and some fuel was found in the line. The gascolator was removed and approximately 7 to 8 ounces of fuel (absent of debris) was recovered. The carburetor was removed and disassembled and approximately 2 ounces of fuel (absent of debris) was observed in the bowl. No mechanical deficiencies were noted with the airplane or engine.
Probable Cause: The flight instructor's failure to monitor the available fuel supply, which resulted in a loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN11CA221 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB CEN11CA221
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 15:16 |
ASN Update Bot |
Added |
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