ASN Wikibase Occurrence # 289653
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Date: | Wednesday 30 October 2013 |
Time: | 20:40 LT |
Type: | Aero Commander 500 - B |
Owner/operator: | Central Air Southwest |
Registration: | N917GT |
MSN: | 500B-1137-77 |
Total airframe hrs: | 24248 hours |
Engine model: | Lycoming IO-540-E1A5 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lubbock, Texas -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | El Paso International Airport, TX (ELP/KELP) |
Destination airport: | Lubbock Preston Smith International Airport, TX (LBB/KLBB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, as the airplane approached the landing airport, he descended through windshear and turbulence before he turned on final; a strong southwest wind caused him to overshoot the final approach segment. The airplane was a "little high and fast," and he was encountering windshear bumps. He reduced engine power and maneuvered back to the runway centerline. He slowed the airplane to landing speed while applying half and then full flaps. The airplane subsequently touched down with the landing gear partially extended. The pilot did not recall seeing the landing gear position lights illuminated green; he further stated that he recited, but did not perform, the landing gear check because he was "very focused" on controlling the airplane through the windshear. He thought he landed the airplane with the gear up, and, at some point during the slide, he instinctively activated the gear handle. He said that he thought that he did not extend the landing gear. Postaccident examination of the landing gear system revealed no evidence of mechanical anomalies that would have precluded normal operation.
Probable Cause: The pilot's failure to complete a landing checklist and extend the landing gear, which resulted in a gear-up landing. Contributing to the accident was the pilot's diverted attention to the weather during approach.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14LA065 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
NTSB CEN14LA065
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 16:38 |
ASN Update Bot |
Added |
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