ASN Wikibase Occurrence # 289659
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 26 October 2013 |
Time: | 12:45 LT |
Type: | Cessna 150H |
Owner/operator: | Private |
Registration: | N684RA |
MSN: | 15068698 |
Year of manufacture: | 1968 |
Total airframe hrs: | 7173 hours |
Engine model: | Continental 0-200 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Livingston, Alabama -
United States of America
|
Phase: | Standing |
Nature: | Private |
Departure airport: | Cullman, AL (KCMD) |
Destination airport: | Gonzales, LA (L38) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After purchasing the airplane, the pilot serviced it with fuel at the self-service pump and then departed on the cross-country flight to his home airport. About 1.4 hours into the flight, he noticed the fuel quantity displayed on the fuel gauges rapidly decreasing and the electrical system "discharging." (Although the pilot reported he had been flying for 45 minutes, based on the takeoff and landing location, the airplane traveled 140 miles; the airplane's cruise speed is 100 mph; therefore, he had been flying about 1.4 hours.) The pilot chose to conduct a precautionary landing to a field. Upon landing, the nose gear dug into the soft soil, and the airplane then nosed over and came to rest inverted, which resulted in substantial damage to the engine firewall. According to the pilot, the engine was running "fine" throughout the flight, and it never stopped producing power.
The pilot recovered and disassembled the airplane before reporting the accident. During recovery, he noted that one of the two 13-gallon fuel tanks was empty and that the other tank contained about 1/4 tank of fuel (about 3 to 4 gallons), which confirmed that his fuel gauges were reading accurately. After the accident, only one fuel cap was recovered from the airplane, and a similar fuel cap was recovered at the self-service pump at the departure airport. Interpolation of performance data revealed that, at a 6 gallon-per-hour fuel consumption rate, the airplane would have consumed about 8 gallons of fuel. With one fuel tank venting overboard and the engine consuming 8 gallons of fuel from the other tank, the airplane would have contained about 4 gallons of fuel at landing.
Probable Cause: The pilot's inadequate soft-field technique during the precautionary landing, which resulted in a nose-over. Contributing to the accident was the pilot's inadequate preflight inspection, which resulted in departure with an open fuel port and the subsequent in-flight, overboard venting of the fuel supply.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA094 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB ERA14LA094
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 16:43 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation