ASN Wikibase Occurrence # 290078
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Date: | Friday 26 April 2013 |
Time: | 16:42 LT |
Type: | Piper PA-28-151 |
Owner/operator: | |
Registration: | N75148 |
MSN: | 28-7615259 |
Year of manufacture: | 1976 |
Total airframe hrs: | 3984 hours |
Engine model: | Lycoming 0-320 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Daytona Beach, Florida -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Daytona Beach, FL (7FL6) |
Destination airport: | Titusville-Space Coast Regional Airport, FL (TIX/KTIX) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After completing an annual inspection of the airplane, the student pilot completed a preflight inspection and notified his flight instructor that he was going to depart. He reported that, while taxiing toward the runway, the engine stalled. He then "shut everything down" and spoke to a mechanic about what had just happened. The mechanic advised him that the fuel selector was in the "OFF" position. The student pilot then moved the fuel selector to the left-tank position. The student pilot then restarted the airplane, taxied onto the runway, and took off.
About 300 feet above ground level, the engine "sputtered." The pilot then leveled off the airplane and the engine restarted, but it lost power again. He then radioed that he was going to make an emergency landing, maintained the best glide speed, and tried to reland on the runway, but he missed the runway due to a "gust of wind" that pushed the airplane right. The pilot then lowered the nose to avoid trees and houses beyond the end of the runway. The airplane touched down right of the runway centerline, skipped once, and then slid to a stop. The airplane sustained substantial damage to the wings and fuselage.
Data recorded by the airplane's onboard engine data monitoring system were consistent with a loss of engine power after takeoff, the power returning, and then a second loss of engine power. A postaccident engine test run did not reveal any preimpact failures or malfunctions that would have precluded normal operation. Fuel was found in both fuel tanks. The atmospheric conditions at the time of the accident were not conducive to the accumulation of carburetor ice.
Probable Cause: A total loss of engine power during initial climb for reasons that could not be determined because postaccident examinations did not reveal any preimpact failures or malfunctions that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA13LA220 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
NTSB ERA13LA220
Location
Revision history:
Date/time | Contributor | Updates |
06-Oct-2022 07:55 |
ASN Update Bot |
Added |
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