ASN Wikibase Occurrence # 290102
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Date: | Sunday 14 April 2013 |
Time: | 15:45 LT |
Type: | Needham Stoddard-Hamilton TD |
Owner/operator: | Private |
Registration: | N95RL |
MSN: | 609 |
Total airframe hrs: | 1064 hours |
Engine model: | Lycoming IO-320-B1A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bloomington, Indiana -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Bloomington-Monroe County Airport, IN (BMG/KBMG) |
Destination airport: | Delphi, IN (1I9) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot lost directional control during the takeoff roll, and the airplane veered off the runway and impacted terrain. A postaccident examination of the flight control system revealed that the right rudder control cable had slipped out of a connector and detached from the bellcrank due to the improper crimping of the connector collar.
Probable Cause: The improper installation of a rudder control cable connector and its subsequent separation from the bellcrank, which resulted in the loss of directional control during takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN13LA231 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB CEN13LA231
Location
Revision history:
Date/time | Contributor | Updates |
06-Oct-2022 10:51 |
ASN Update Bot |
Added |
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