Accident Velocity XL RG N101ME,
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ASN Wikibase Occurrence # 290111
 
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Date:Friday 12 April 2013
Time:09:55 LT
Type:Silhouette image of generic VELO model; specific model in this crash may look slightly different    
Velocity XL RG
Owner/operator:private
Registration: N101ME
MSN: 3RX025
Year of manufacture:2003
Total airframe hrs:30 hours
Engine model:Lycoming IO-540-K1H5
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Avon Park, Florida -   United States of America
Phase: En route
Nature:Private
Departure airport:Fort Lauderdale-Executive Airport, FL (FXE/KFXE)
Destination airport:Plant City Municipal Airport, FL (KPCM)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot and the pilot-rated passenger departed for the destination airport with about 50 gallons of fuel on board. About 35 minutes into the flight, they heard a "pop." They then scanned the instruments and noted that everything looked good. A short time later, they heard additional "pop" sounds. The pilot then began descending the airplane from 4,500 ft mean sea level (msl) to get under the clouds for a "better visual," and, when the airplane was about 2,000 ft msl, the pilot increased the mixture control to full rich and turned the boost pump on. He then looked at the exhaust gas temperature (EGT) display and noticed that three of the cylinders "had gone cold." The engine then began losing power and running roughly. At this point, he decided to divert, and, as he turned the airplane toward the diversion airport, the engine lost all power. The pilot decided to land on a road. After touching down, he headed the airplane off the road to the right to avoid a car, and the airplane went down the shoulder. The right wing got caught in the grass, which caused the airplane to veer right. The airplane then struck a barbed wire fence and was substantially damaged.

Review of data stored in the onboard engine analyzer indicated that the cylinder head temperature and EGT for all of the engine's cylinders dropped over about a 5-minute period in the following order: No. 5, No.3, No. 4, No.1, No. 2, and No. 6, which is typically indicative of a fuel or ignition problem. However, examination and testing of the ignition system did not reveal any damage, unusual wear conditions, or evidence of significant contamination, and all of the ignition components successfully passed new part performance checks. No conditions were found that would have prevented normal ignition operation. Additionally, due to the duration of the loss of engine power and the fact that the ignition system had dual magnetos, it was unlikely that an ignition system problem caused the power loss.

Examination of the fuel system revealed that, at the time of the accident, the airplane still had about 40 gallons of clean fuel onboard. Examination and testing of the fuel injection system and engine did not reveal evidence of any preimpact failures or malfunctions. After the examination of the engine and replacement of parts damaged during the accident, the engine was started and an engine test run was conducted with no anomalies noted.

According to the airplane's flight manual, modern aircraft engines are extremely durable and seldom fail catastrophically without plenty of advance warning (lowering oil pressure, excessive mechanical noise, rising oil temperature, etc.). However, since none of these conditions were reported by the pilot and postaccident examinations of the ignition, fuel injection, and lubrication systems, as well as the mechanical components of the engine, determined that they were functional at the time of the accident, the reason for the engine failure could not be determined.

Probable Cause: A total loss of engine power during cruise flight for reasons that could not be determined because postaccident examination and testing did not reveal any mechanical malfunctions or failures that would have precluded normal operation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA13LA204
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

NTSB ERA13LA204

History of this aircraft

Other occurrences involving this aircraft
16 February 2018 N551ZL Private 0 Locust Grove, GA sub
Gear-up landing
1 February 2024 N551ZL Private 0 Atlanta Speedway Airport, GA (KHMP) unk

Location

Revision history:

Date/timeContributorUpdates
06-Oct-2022 10:57 ASN Update Bot Added
01-Aug-2023 21:24 harro Updated

Corrections or additions? ... Edit this accident description

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