ASN Wikibase Occurrence # 290113
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Date: | Thursday 11 April 2013 |
Time: | 14:00 LT |
Type: | Progressive Aerodyne SeaRey |
Owner/operator: | |
Registration: | N92319 |
MSN: | 1DK109 |
Total airframe hrs: | 550 hours |
Engine model: | Rotax 912S |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Polk City, Florida -
United States of America
|
Phase: | Taxi |
Nature: | Private |
Departure airport: | Polk City, FL |
Destination airport: | Groveland, FL (3FD4) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, he taxied the amphibious airplane down a boat ramp following a vintage twin-engine amphibious airplane that weighed more than 6,000 pounds. The other airplane took off, and the accident airplane then encountered a 2- to 3-foot water wake. The pilot "quartered" his airplane into the wake, and, subsequently, the right side pitched up, and the left side pitched down. The pilot then looked at the left horizontal stabilizer via a mirror on the airplane's left wing strut, conducted a full flight control check, and noted no anomalies. The pilot then began the takeoff, and the airplane bounced once along the choppy water surface before becoming airborne. Once airborne, the pilot noted pitch control problems and was not able to level the airplane until it reached about 1,800 feet. He was then able to descend the airplane at a rate of about 50 feet per minute by maintaining airspeed just above stall. The pilot circled the lake six times before being able to land. Upon landing, the right wing bounced twice, and, during the second bounce, the right horizontal stabilizer was substantially damaged when it dragged through the water.
Postaccident examination of the airplane revealed a broken outboard left horizontal stabilizer tube that likely broke during the wake encounter. The examination also revealed that the bolt connecting three stabilizer cables had torn into the fabric, which likely resulted in the control stick binding in a pitch-up position upon rotation.
Probable Cause: An inadvertent encounter with the water wake from a larger amphibious airplane before takeoff and the pilot's subsequent inadequate preflight inspection of the airplane during which he failed to note damage caused by the wake encounter.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA13LA198 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB ERA13LA198
Location
Revision history:
Date/time | Contributor | Updates |
06-Oct-2022 11:03 |
ASN Update Bot |
Added |
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