Runway excursion Accident Piper PA-23-250 N318CA,
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ASN Wikibase Occurrence # 290142
 
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Date:Monday 18 March 2013
Time:14:15 LT
Type:Silhouette image of generic PA27 model; specific model in this crash may look slightly different    
Piper PA-23-250
Owner/operator:
Registration: N318CA
MSN: 27-2908
Year of manufacture:1965
Total airframe hrs:5009 hours
Engine model:Lycoming IO-540
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Hillsboro, Oregon -   United States of America
Phase: Take off
Nature:Training
Departure airport:Hillsboro, OR (7S3)
Destination airport:Hillsboro, OR (7S3)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight was to be the private pilot's first multiengine lesson. Both he and the instructor performed an uneventful preflight check and run-up, which included a check of the brakes and the security of the cabin door. During the takeoff roll, the cabin door opened, and the flight instructor called for the pilot to abort the takeoff. The pilot reduced engine power to idle and applied pressure to the brake pedals. The airplane began to decelerate; however, as it approached the end of the runway, brake effectiveness began to dissipate, and the airplane travelled beyond the threshold, coming to rest in a ditch.

The airplane was equipped with foot-operated brakes on the left side only, which was occupied by the pilot undergoing instruction. The remaining runway distance, had it been flat, should have provided for an adequate distance to stop; however, the runway sloped downhill, with its gradient rapidly increasing beyond the threshold. It is likely that this increased downsloping gradient resulted in an increased distance needed to stop the airplane.

Postaccident examination of the braking system revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation.

Probable Cause: A runway overrun due to an insufficient stopping distance due to the downsloping runway during a rejected takeoff. Contributing to the accident was a cabin door that inadvertently opened during the takeoff roll.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR13LA154
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB WPR13LA154

Location

Revision history:

Date/timeContributorUpdates
06-Oct-2022 11:21 ASN Update Bot Added

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