Accident Hughes 369HS N193M,
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ASN Wikibase Occurrence # 290212
 
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Date:Tuesday 29 January 2013
Time:09:30 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 369HS
Owner/operator:Daniel Mills
Registration: N193M
MSN: 1190219S
Year of manufacture:1969
Total airframe hrs:6309 hours
Engine model:Allison 250-C18
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:London, Ohio -   United States of America
Phase: En route
Nature:Private
Departure airport:Canton, OH
Destination airport:Dayton-James Cox Dayton International Airport, OH (DAY/KDAY)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The private pilot said the helicopter's turbine engine lost power after flying through an area of moderate to heavy snow. The pilot entered an autorotation and applied excessive aft cyclic during the touchdown in a field, which caused the main rotor blades to flex down and sever the tailboom. Weather reported in the area included snow and freezing fog, with a temperature of 16 degrees F. The helicopter was equipped with an automatic engine re-ignition and engine failure warning system, which was required per the rotorcraft flight manual (RFM) for operation in falling or blowing snow. The pilot said this system was armed at the time of the engine failure and the engine-out warning light illuminated and an audible tone sounded before the power loss. The RFM also stated that flight into known icing conditions was prohibited and fuel had to meet anti-icing capability of JP-4 when operating at 40 degrees or less. A review of fueling records revealed that no anti-icing additive was added to the fuel. The pilot was aware of the icing conditions, but he continued the flight. Examination of the engine found no mechanical anomalies that would have precluded normal operation.

Probable Cause: The pilot's failure to comply with established cold weather operating procedures, which resulted in a total loss of engine power. Contributing to the accident was the pilot's excessive aft cyclic input during the landing flare, which resulted in main rotor blade contact with the tail boom.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN13CA145
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB CEN13CA145

Location

Revision history:

Date/timeContributorUpdates
06-Oct-2022 12:14 ASN Update Bot Added

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