ASN Wikibase Occurrence # 290228
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Date: | Friday 11 January 2013 |
Time: | 23:30 LT |
Type: | American General AG-5B Tiger |
Owner/operator: | |
Registration: | N897GA |
MSN: | 10076 |
Total airframe hrs: | 4519 hours |
Engine model: | Lycoming O-360-A4K |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ankeny, Iowa -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Cape Girardeau Airport, MO (CGI/KCGI) |
Destination airport: | Ankeny Regional Airport, IA (IKV/KIKV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that before arriving at his destination airport in night visual meteorological conditions, he listened to the automated weather observing system, which indicated wind from 220 degrees at 10 knots, gusting to 26 knots. The pilot aborted his first attempt to land after a bounced landing. During the second approach to land, the pilot observed the visual approach slope indicator rapidly transition from both white (indicating high on the glideslope) to both red (indicating low on the glideslope) and decided to perform a go-around. During the attempted go-around, the airplane's left wing struck a tree, which resulted in substantial damage to the left wing and horizontal stabilizer. The pilot then landed the airplane without further incident on his third landing attempt. The pilot stated that the airplane's interior lighting was too bright for the night conditions and that the bright runway lights in the dark rural setting gave him a 'false sense of night vision.â€
Probable Cause: The pilot's failure to maintain a proper glide path to the runway in gusty wind conditions and his failure to maintain clearance from obstructions during the subsequent go-around. Contributing to the accident was the pilot's improper interior lighting configuration.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN13CA133 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB CEN13CA133
Location
Revision history:
Date/time | Contributor | Updates |
06-Oct-2022 12:26 |
ASN Update Bot |
Added |
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