Accident Mooney M20C N6242U,
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ASN Wikibase Occurrence # 290230
 
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Date:Thursday 10 January 2013
Time:10:30 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C
Owner/operator:
Registration: N6242U
MSN: 2081
Year of manufacture:1962
Total airframe hrs:5500 hours
Engine model:Lycoming O-360-A1D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Moriarty, New Mexico -   United States of America
Phase: Standing
Nature:Private
Departure airport:Moriarty, NM (0E0)
Destination airport:Moriarty, NM
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Before the accident flight, the pilot purchased 30 gallons of aviation gasoline, following which the fuel gauges indicated near half for each tank. During the accident flight, the pilot flew about 12 minutes south of the departure airport with the left fuel tank selected then turned north to return to the airport. About 5 minutes after turning north, the engine went to idle power. The pilot turned the carburetor heat on and activated the boost pump, and the engine returned to normal cruise power. The pilot indicated that, at this point, she should have switched the fuel selector valve to the right fuel tank but did not. The engine operated at cruise power for about 1 minute then quit completely. The pilot reported that because the airplane was about 1,500 feet above ground level and changing the fuel selector valve requires moving the pilot seat back about 18 inches 'with no control of the aircraft,” she decided to perform a forced landing on a farm road directly ahead. During the landing, the right wing struck a fence post, and the airplane subsequently came to rest in a plowed field. Both wings sustained substantial damage. The pilot reported that the accident was caused by fuel starvation and that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

Probable Cause: The pilot's improper fuel management, which resulted in a loss of engine power during cruise flight due to fuel starvation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN13CA134
Status: Investigation completed
Duration: 2 months
Download report: Final report

Sources:

NTSB CEN13CA134

Location

Revision history:

Date/timeContributorUpdates
06-Oct-2022 12:26 ASN Update Bot Added

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