ASN Wikibase Occurrence # 290597
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Date: | Thursday 22 May 2014 |
Time: | 18:30 LT |
Type: | P&M Aviation QUIKR |
Owner/operator: | Private |
Registration: | N428PM |
MSN: | 8428 |
Year of manufacture: | 2009 |
Total airframe hrs: | 182 hours |
Engine model: | Rotax 912 ULS |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Minor |
Category: | Accident |
Location: | Gulf Shores, Alabama -
United States of America
|
Phase: | Standing |
Nature: | Private |
Departure airport: | Gulf Shores-Edwards Airport, AL (GUF/KJKA) |
Destination airport: | Gulf Shores-Edwards Airport, AL (GUF/KJKA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot attempted to start the weight-shift-aircraft's engine in an area surrounded by hangars. After about eight attempts to start the engine, it finally engaged and immediately advanced to takeoff power. The aircraft then collided with a parked airplane about 150 ft from its original starting position, spun right, impacted a hangar door, and came to rest. Postaccident examination of the throttle system revealed no mechanical anomalies that would have precluded normal operation. Although two throttle cable snag hazards were identified that could have resulted in a stuck throttle, it could not be determined if either possible hazard caused the throttle to become stuck in the open position. According to the Pilot's Operating Handbook (POH), the aircraft should have been pointing away from people, vehicles, or buildings during startup. The POH also stated that, if the engine does not start after five or six attempts, the pilot should switch the ignition off and investigate the cause of the problem.
Probable Cause: The pilot's failure to maintain aircraft control during engine startup, which resulted in a collision with a parked airplane. Contributing to the accident was the pilot's failure to follow engine startup procedures and a sudden surge of engine power for reasons that could not be determined because postaccident examination did not reveal any mechanical malfunctions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA257 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB ERA14LA257
Location
Revision history:
Date/time | Contributor | Updates |
06-Oct-2022 17:06 |
ASN Update Bot |
Added |
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