ASN Wikibase Occurrence # 290984
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Date: | Saturday 20 June 2015 |
Time: | 12:30 LT |
Type: | Paquin Michael A A gyroplane |
Owner/operator: | |
Registration: | N485MP |
MSN: | 1-2011 |
Year of manufacture: | 2012 |
Total airframe hrs: | 95 hours |
Engine model: | Compact Radial Engines MZ202 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Concord, New Hampshire -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Concord Airport, NH (CON/KCON) |
Destination airport: | Concord Airport, NH (CON/KCON) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot of the amateur built gyrocopter reported that during taxi to the runway, he was distracted by his electronic altimeter when it entered a sleep mode. After resetting the altimeter, the pilot immediately entered the active runway and initiated the takeoff roll without disengaging the main rotor brake. Subsequently, at 25 miles per hour during the takeoff roll he reported an unusual vibration and a knocking sound. The pilot attempted to reduce speed, but the gyrocopter tipped forward and to the left, the main rotor impacted the ground, and the gyrocopter rolled over on its right side coming to a stop on the runway.
During an interview with the pilot, he explained that the rotor brake must be disengaged before takeoff. He also stated that this accident may have been prevented if the rotor brake was designed in a manner that required manual hand pressure from the pilot.
The pilot stated there were no mechanical malfunctions or failures with the gyrocopter that would have precluded normal operation. Substantial damage was found along the main rotor and vertical stabilizer.
Probable Cause: The pilot's inability to maintain directional control during takeoff, which resulted in a roll over. Contributing to the loss of control was the pilot's failure to disengage the main rotor brake prior to takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA15CA127 |
Status: | Investigation completed |
Duration: | 1 month |
Download report: | Final report |
|
Sources:
NTSB GAA15CA127
Location
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 08:06 |
ASN Update Bot |
Added |
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