ASN Wikibase Occurrence # 291593
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 2 December 2006 |
Time: | 11:30 LT |
Type: | Stits SA-6B Flut-R-Bug |
Owner/operator: | |
Registration: | N3129 |
MSN: | 99583 |
Total airframe hrs: | 414 hours |
Engine model: | Continental A80 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Camerson, Texas -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Camerson, TX |
Destination airport: | Camerson, TX |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:With the eventual goal of earning a sport pilot certificate, an ultralight pilot and a 1,141-hour flight instructor planned to conduct a familiarization training flight in an experimental, tandem seat airplane. During the take-off roll, with the ultralight pilot occupying the front seat and operating the controls, the airplane "ballooned." The ultralight pilot reduced engine power and performed a normal landing. During the second take-off from Runway 16 (a 3,200-foot long by 50-foot wide asphalt runway), "the airplane ballooned more than before" and the pilot elected to reduce the engine power and land. The ultralight pilot stated that "the flare did not fully develop and [the airplane] landed harder than usual." During the landing, the right main landing gear and the nose landing gear collapsed. In the Recommendation section of the NTSB Form 6120.1, (How could this accident have been prevented ?), the ultralight pilot stated that the accident could have been prevented " with the judicious use of throttle in the flare, or if I had carried more airspeed to compensate for the possible loss of a gusting headwind." The winds at the time of the accident were reported as variable at 8 knots.
Probable Cause: The pilot's improper landing flare and inadequate recovery from a bounced landing which resulted in a hard landing. A factor was the delayed remedial action by the flight instructor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW07CA033 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB DFW07CA033
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 16:39 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation