ASN Wikibase Occurrence # 291644
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Date: | Tuesday 14 November 2006 |
Time: | 15:55 LT |
Type: | Mooney M20J |
Owner/operator: | |
Registration: | N202WB |
MSN: | 24-0261 |
Year of manufacture: | 1977 |
Total airframe hrs: | 3902 hours |
Engine model: | Lycoming IO-360-A1B6D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Akron, Ohio -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Wadsworth, OH (15G) |
Destination airport: | Akron/Canton Regional Airport, OH (CAK/KCAK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was substantially damaged when it impacted the runway during landing. The pilot reported that he deployed full flaps during the right turn from base leg to final approach. He stated that upon rolling out of the turn on final, he realized that the flaps were not symmetrically deployed. He added that the right flap was full down, but the left flap was only partially down. He attempted to raise the flaps; however, they became jammed asymmetrically. He stated that "as I rolled out for the flare, the left wing stalled and dropped sharply. I attempted to add power which only temporarily lifted the left wing. With the right wing generating significant lift and the left wing not, a steep left turn and loss of control resulted." A post accident examination confirmed flap system continuity. In addition, the flap actuator motor operated when electrical power was applied. Impact damage precluded an exact measurement of the flap deflections and rigging. The pilot noted that he had experienced an asymmetric extension and jammed flap situation about 2 months prior to the accident. He reported that in that instance he had maintained additional airspeed on approach and landed safely. He reported that subsequent maintenance action had resolved the problem and he had not experienced any further flap problems until the accident flight.
Probable Cause: The pilot's failure to maintain sufficient airspeed during final approach resulting in an inadvertent stall. Contributing factors were the airplane's low altitude at the time of the stall and the asymmetric flap configuration.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI07CA023 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB CHI07CA023
History of this aircraft
Other occurrences involving this aircraft
28 August 1993 |
N202WB |
Southland Fire Place Shop, Inc |
0 |
Kelley's Island, OH |
|
sub |
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 17:15 |
ASN Update Bot |
Added |
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