ASN Wikibase Occurrence # 292010
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Date: | Wednesday 26 July 2006 |
Time: | 07:05 LT |
Type: | Beechcraft A36 |
Owner/operator: | Private |
Registration: | N9205Q |
MSN: | E-271 |
Year of manufacture: | 1971 |
Engine model: | Continental IO-520 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mason, Michigan -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Mason Jewett Field, MI (KTEW) |
Destination airport: | Georgetown, KY (27K) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane contacted a building and two parked vehicles after takeoff. The pilot reported that everything during the preflight engine run up was normal. He reported he rotated the airplane at 80 knots during the takeoff and pitched 10 degrees nose up to achieve the best angle of climb. The pilot reported the initial climb to about 150 feet above the ground was normal, then the airplane hesitated and stopped climbing. He reported the airplane then climbed slowly for a couple of seconds prior to it starting a descent. The pilot reported the airspeed decreased, the stall warning sounded, and the airplane began to buffet. The pilot lowered the nose and made a slight right turn to avoid obstacles. He stated he wanted to bank further to the right, but there were two telephone poles along the flight path. He stated the right wing of the airplane struck a building mounted antenna as he reduced the engine power. The landing gear then contacted the roof of a building and two parked vehicles prior to impacting a parking lot. The pilot and passengers exited the airplane before it was destroyed by a post impact fire. The pilot reported, "In summary, there appeared to be a partial loss of power during the initial climb." Post accident inspection of the engine failed to reveal any mechanical failure/malfunction.
Probable Cause: The pilot's failure to maintain adequate airspeed which resulted in a stall/mush on takeoff. Factors associated with the accident were the building and vehicles that were contacted.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI06CA201 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB CHI06CA201
Revision history:
Date/time | Contributor | Updates |
08-Oct-2022 13:23 |
ASN Update Bot |
Added |
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