Accident Hughes 369A N72LB,
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ASN Wikibase Occurrence # 292101
 
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Date:Thursday 6 July 2006
Time:15:55 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 369A
Owner/operator:John Holmes
Registration: N72LB
MSN: 691194
Year of manufacture:1969
Total airframe hrs:4405 hours
Engine model:Allison 250-C10D
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Medford, Oregon -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Medford, OR
Destination airport:Jacksonville, OR
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot said that he flew a high reconnaissance circle over his intended landing site. He observed ripples on a pond which led him to believe that the wind was from the south. During his landing approach, as he descended to 10 to 15 feet AGL, he pulled up on the collective to extend his glide. The pilot said the helicopter started to settle and became very unstable. He "recognized it as settling with power down wind." He leveled the skids and the helicopter hit the ground; he said that 1 or 2 seconds later the helicopter began to lift and turn to the right. He applied left pedal with no response; he then lowered the collective. Subsequently, the left skid tube caught the ground and collapsed, and the helicopter came to rest on its left side. The main rotor blades did not come in contact with the ground or any part of the helicopter, but the tail rotor blades were broken. Additionally the tail boom and tail rotor drive shaft were broken. The pilot said that after he got out of the helicopter, he noticed that the wind was variable with light gusts. He said that the pond was being filled with water which gave him an incorrect interpretation of the wind conditions for landing.

Probable Cause: The pilot's misinterpretation of the wind direction (in-flight planning) and subsequent improper descent rate to the ground during a landing attempt. A factor was the tailwind conditions.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA06CA137
Status: Investigation completed
Duration: 3 months
Download report: Final report

Sources:

NTSB SEA06CA137

Revision history:

Date/timeContributorUpdates
08-Oct-2022 14:28 ASN Update Bot Added

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