Accident Mooney M20J N511G,
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ASN Wikibase Occurrence # 292597
 
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Date:Wednesday 1 March 2006
Time:12:40 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20J
Owner/operator:Private
Registration: N511G
MSN: 24-1207
Year of manufacture:1981
Total airframe hrs:3525 hours
Engine model:Lycoming IO-360-3B6D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Fort Pierce, Florida -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Fort Pierce-Saint Lucie County Airport, FL (FPR/KFPR)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that about 8 to 10 minutes after takeoff, while still climbing, at an altitude of about 5,000 feet, the airplane lost engine power. The pilot further stated that the gauges showed about 1,000 rpm, and the manifold pressure remained at 25 inches. He turned around and returned to the airport and made attempts to restart the engine, all of which were unsuccessful. The pilot made a forced landing to a clearing short of the airport property, and the airplane incurred substantial damage. A postcrash examination of the airplane revealed that the dual magneto had detached from its mounted position, and was hanging by the ignition harness behind the engine. The magneto had not incurred any damage, and the magneto drive gear was laying in the accessory housing along with one hold-down plate. The retaining nuts, washers and lock washers were not recovered. When tested, the magneto operated on all eight distributor outputs. The impulse coupler was not damaged, and the distributor wiring was intact. There was engine continuity, proper valve action, and compression on all cylinders. Engine oil was present, and there was evidence of some oil having leaked at the back of the engine. No anomalies were noted with either the induction or fuel systems. The airplane had last received an annual inspection on August 2005 when an overhauled engine had been installed. It had accumulated 10 hours since the annual inspection.

Probable Cause: Improper magneto installation by maintenance personnel, which resulted in the magneto detaching from the engine and subsequent loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA06LA058
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB MIA06LA058

Revision history:

Date/timeContributorUpdates
09-Oct-2022 06:38 ASN Update Bot Added

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