Accident Piper PA-28RT-201T N2939V,
ASN logo
ASN Wikibase Occurrence # 292604
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 25 February 2006
Time:08:45 LT
Type:Silhouette image of generic P28T model; specific model in this crash may look slightly different    
Piper PA-28RT-201T
Owner/operator:
Registration: N2939V
MSN: 28R-7931264
Year of manufacture:1979
Total airframe hrs:3817 hours
Engine model:Teledyne Continental TSIO-360-FB5B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Parker, Colorado -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Denver-Front Range Airport, CO (KFTG)
Destination airport:BUENA VISTA, CO (7V1)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that during cruise flight the engine rpm increased to an "over speed condition." When he increased power, he could not keep the rpm under redline and he elected to perform a forced landing. During the landing, the landing gear collapsed resulting in substantial damage. The pilot stated they had been having difficulty obtaining full rpm from the engine. He stated that the propeller governor had been adjusted several times, but full rpm was never obtained. On November 16, 2005, at an engine tachometer time of 1,959.37, the oil and filter were removed and replaced, and an oil sample was sent for analysis. The results from that analysis indicated "excessive wear." Removal of the oil suction screen revealed metal contamination inside and outside the screen. Examination of the propeller governor revealed the adjustment screw had been adjusted beyond its maximum stop. The propeller governor was removed and the screen between the governor and the engine was entirely obstructed with metal contamination. Removal and examination of the oil filter revealed metal contamination. Broken portions of the number two main bearing were found within the oil sump. Breakaway torque values revealed that the number two and number three cylinder throughbolt nuts, at the cylinder flange, were loose at 500 inch/pounds. Further examination revealed metal contamination throughout the engine, including the oil pump and the oil cooler. No other anomalies were noted with the airframe, propeller, or engine.



Probable Cause: the improper maintenance procedures resulting in the unseating of the number two main bearing. Contributing factors include the mechanic's improper troubleshooting procedures, and the pilot's improper decision to continue operating the airplane with known internal excessive engine wear, and engine rpm issues.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN06LA044
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB DEN06LA044

Revision history:

Date/timeContributorUpdates
09-Oct-2022 06:44 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org