ASN Wikibase Occurrence # 292605
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Date: | Friday 24 February 2006 |
Time: | 14:20 LT |
Type: | Cessna 150G |
Owner/operator: | Private |
Registration: | N6366S |
MSN: | 15067166 |
Year of manufacture: | 1967 |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Rockford, Ohio -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Battle Creek-WK Kellogg Regional Airport, MI (BTL/KBTL) |
Destination airport: | Phillipsburg, MI (3I7) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Cessna 150G experienced a total loss of engine power during cruise flight in visual meteorological conditions. The pilot attempted an emergency landing to a private airstrip. The passenger stated that the pilot realized the airplane was too high during the approach, so the pilot pushed the nose over to descend more quickly. The passenger stated that the airplane touched down on a field west of the airstrip at a speed of approximately 70 knots. The pilot pulled back on the yoke in order to avoid trees and a house. The airplane then climbed, stalled, and impacted electrical wires. The airplane then impacted trees and hit a berm. The airplane was not equipped with shoulder harnesses. On-scene inspection of the airplane revealed that there was less than one gallon of fuel recovered from the left tank, and no fuel was recovered from the right tank. The fuel tanks were not broken open, and no fuel leaks were noted.
Probable Cause: The fuel exhaustion due to the inadequate preflight planning/preparation by the pilot-in-command. Additional causes were the inadequately planned approach and improper emergency procedure by the pilot-in-command.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI06LA087 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB CHI06LA087
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 06:44 |
ASN Update Bot |
Added |
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